I found leakage & clogs in my system which would attribute to the crappy mileage.
I used my eudiometer to check my production at the intake. For some reason it was .25 LPM.
Digging I found several issues. First my lovely reservoir leaked gas from the cap. I suspected in as much as that was the only part that was not in my bench setup. I swapped it out for the other one for now.
I also disconnected the circulating pump since my cell is relatively cool. Ok so then I blew air into the line from the reservoir to the bubbler, nothing. Can't blow the air into it. Why? The stone is clogged beyond use. I replaced it and ran the truck.
I see real good gas production at the reservoir. I test it at the intake... 2 LPM.
The scangauge is reading better mileage but still not as good as without HHO.
Filled up my mileage went from 15.5 MPG to 12.4 MPG.
I also threw an 1151 & a 1131 code (lean condition) My EFIE was set to 338MV I suppose this is due to the fact that not much HHO was getting into the intake.
I have to play with the EFIE now, maybe set it to around 355mv.
Tuesday, May 25, 2010
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